Fr. Lower Inbd Control Arm Bolts (91 Civic)

Discussion in 'Civic' started by Elle, Apr 30, 2006.

  1. Elle

    Elle Guest

    Has anyone had success freeing these without shearing off
    the bolt head?

    I PB Blastered what I could, then I put some torque on the
    bolt head this afternoon. I didn't have a good angle and
    didn't want to push it just yet.

    The nut on the back side of the bolt appears to be welded to
    the frame. I don't want to bust the nut just yet, because of
    experience with doing this on one of the rear control arms.

    I am supporting the car at the usual side jacking points
    with two jackstands. Might I get an advantage freeing these
    bolts supporting the engine (via a jack, some blocks of wood
    pushing up on the oil pan)? I'm thinking the weight of the
    engine is still acting at least partly on the bushing and
    bolt.

    If the heads are likely to shear off, I'm thinking of
    running it to my favorite import shop and having them
    replace them. My tool collection is just too amateurish to
    go at this effectively (based on experience with my rear
    control arm bolts), and I sure don't like the tight space
    under which I must work for these ones.

    The front lower outboard control arm bolts came off easily.

    This contrasts with the rear lower control arms, where the
    inbds came off pretty easily, while I sheared off the heads
    of the outboard ones.

    Update on my other suspension renovation efforts:
    Team Honda (= cheapesthondaparts.com) in Colorado came
    through, though it might be because I called them twice in
    eight days to see why my order wasn't being tracked online
    per their web site's description. I installed their brand
    new front suspension springs and stabilizer bar links and
    bushings yesterday. The Harbor Freight Spring Compressor
    tool gets easier to use every time, as I learn its
    idiosyncrasies. The old springs, when relaxed, were a little
    longer than the new ones (relaxed) by about one-quarter
    inch. OTOH, the new springs raised the car's height around
    1/2-inch. The car is still not level. I continue to think
    it's a bushing problem. Today's effort was more, slow
    progress towards possibly changing the bushings out. If I
    can get over the control arm bolt hurdle, next I'll purchase
    the ball joint separator tool previously discussed, separate
    the joints, and inspect.

    Oh, discovered a badly torn boot where the gear shift rod
    beneath the car meets the transaxle housing. Doesn't look
    too bad to replace. Nor does it seem too critical.
     
    Elle, Apr 30, 2006
    #1
  2. Elle

    Eric Guest

    Have you tried a short breaker bar, such as an 18" long 1/2" drive?
    Correct, it's a captive nut. That should be one of the points where you're
    spraying the PB Blaster. Also try to get some on the bolt shaft where it
    goes through the bushing.
    I don't think there will be any benefit from jacking up the car via the
    engine. Moreover, you'll be putting quite a bit of strain on the motor
    mounts as well as the oil pan.

    You could always try tapping on the face of the bolt head with a brass punch
    or brass hammer. This may help to loosen it and shouldn't damage the head
    too much.

    Once you get the bolts free, apply some antiseize compound to the bolt shank
    as well as the threads. I like to use the copper based compound but I'm
    sure that opinions will vary on this point.

    Eric
     
    Eric, Apr 30, 2006
    #2
  3. Elle

    Eric Guest

    Have you tried a short breaker bar, such as an 18" long 1/2" drive?
    Correct, it's a captive nut. That should be one of the points where you're
    spraying the PB Blaster. Also try to get some on the bolt shaft where it
    goes through the bushing.
    I don't think there will be any benefit from jacking up the car via the
    engine. Moreover, you'll be putting quite a bit of strain on the motor
    mounts as well as the oil pan.

    You could always try tapping on the face of the bolt head with a brass punch
    or brass hammer. This may help to loosen it and shouldn't damage the head
    too much.

    Once you get the bolts free, apply some antiseize compound to the bolt shank
    as well as the threads. I like to use the copper based compound but I'm
    sure that opinions will vary on this point.

    Eric
     
    Eric, Apr 30, 2006
    #3
  4. Elle

    Elle Guest

    Great. That helps to know.
    I was trying to squeeze in my 2-foot long, 1/2-inch drive
    today but found I needed more height. I'm going to drive my
    car onto my rhino ramps this week and try again.
    I was holding off on spraying into the bushing area until I
    was sure I was going to try to replace the control arm
    bushings this year.

    But I guess the PB Blaster really couldn't do any more
    damage to these 16-year-old, northern U.S. driven, bushings.
    I understand. I am a believer in vibrations helping knock
    free bolts from at least nuts. If it's frozen to the
    bushing, though... Worth a try, for sure, anyway.
    I have both right now. Will go for the copper with at least
    the inbd bolts.

    Thanks again for your assistance, Eric. If I can get the
    bolts free, and then figure out what to do about actually
    removing the old bushings (buy a press or find a shop), and
    then get them all replaced, it will be a real coup. (And not
    totally for fun: I think my uneven tire wear in the right
    front is surely not being helped by these beat up bushings.)
     
    Elle, Apr 30, 2006
    #4
  5. Elle

    Elle Guest

    Great. That helps to know.
    I was trying to squeeze in my 2-foot long, 1/2-inch drive
    today but found I needed more height. I'm going to drive my
    car onto my rhino ramps this week and try again.
    I was holding off on spraying into the bushing area until I
    was sure I was going to try to replace the control arm
    bushings this year.

    But I guess the PB Blaster really couldn't do any more
    damage to these 16-year-old, northern U.S. driven, bushings.
    I understand. I am a believer in vibrations helping knock
    free bolts from at least nuts. If it's frozen to the
    bushing, though... Worth a try, for sure, anyway.
    I have both right now. Will go for the copper with at least
    the inbd bolts.

    Thanks again for your assistance, Eric. If I can get the
    bolts free, and then figure out what to do about actually
    removing the old bushings (buy a press or find a shop), and
    then get them all replaced, it will be a real coup. (And not
    totally for fun: I think my uneven tire wear in the right
    front is surely not being helped by these beat up bushings.)
     
    Elle, Apr 30, 2006
    #5
  6. Elle

    Elle Guest

    (91 Civic LX, 176k miles, rebuilding suspension, with an eye
    to replacing control arm bushings in particular.)

    Yesterday I got the pass. side bolt free. Putting the front
    of the car on my rhino ramps helped; it bought me a lot more
    space to apply lever arm. I applied PB Blaster as best I
    could to both ends, especially the threaded one, and in the
    bushing area as accessible. I used an 18-inch (not 2-foot)
    breaker bar with a 1-foot extension. A six-sided, high
    quality 14 mm socket is a must. (Destroyed one cheap-o
    six-sided socket in the process, but not with any
    catastrophic consequences to property or body.) The bolt
    didn't "break" free, loudly and suddenly, as some rusted
    bolts tend to. It came free very slowly, such that I thought
    I was in fact shearing the head off. But no, I checked the
    other end, and the bolt was moving. I tapped on both ends as
    best I could, often, too, to help free it. After one turn or
    so, I put a 14-mm combination wrench (closed end) on the
    bolt, doubled it up with my 15 mm combination wrench to get
    more lever arm, and unscrewed the bolt until its end was
    flush with the fixed nut. It was very difficult the whole
    time; pretty hard on the arms, even using pipe etc.
    extensions. I sprayed more PB Blaster into the now exposed
    threads of the nut. Pushed some anti-seize in, and
    re-tightened it. I didn't want to take the bolt out all the
    way, because I thought it possible a part of the car would
    collapse.

    The driver's side bolt had the disadvantage of having the
    oil pan in the way, so I couldn't use the 18-inch breaker
    bar. Eventually I just used the roughly six-inch long 14-mm
    combination wrench (closed end) and a scissors jack (resting
    on some plywood) on its end, tapping on the combination
    wrench throughout to ensure it stayed in place 'round the
    bolt. I shot some spray paint at the bolt end this time to
    make it easier to see the bolt moving. It too came free very
    slowly, but surely. The scissors jack wasn't resisting being
    raised all that much, so I didn't feel it was unsafe, though
    of course I took precautions (safety glasses; thick leather
    gloves at one point; a board between me and the setup for
    awhile). After getting a revolution out of the bolt, I did
    the rest by hand, hanging onto a sturdy part of the exhaust
    pipe at times for leverage.

    Didn't even bother torque-wrenching everything afterwards.
    From experience I feel pretty confident I applied over 43
    ft-lbs (the spec for these bolts).

    Tomorrow I hope to narrow down my ball joint lifter tool
    choices (based on counsel here) and possibly order one.
     
    Elle, May 3, 2006
    #6
  7. Elle

    Elle Guest

    (91 Civic LX, 176k miles, rebuilding suspension, with an eye
    to replacing control arm bushings in particular.)

    Yesterday I got the pass. side bolt free. Putting the front
    of the car on my rhino ramps helped; it bought me a lot more
    space to apply lever arm. I applied PB Blaster as best I
    could to both ends, especially the threaded one, and in the
    bushing area as accessible. I used an 18-inch (not 2-foot)
    breaker bar with a 1-foot extension. A six-sided, high
    quality 14 mm socket is a must. (Destroyed one cheap-o
    six-sided socket in the process, but not with any
    catastrophic consequences to property or body.) The bolt
    didn't "break" free, loudly and suddenly, as some rusted
    bolts tend to. It came free very slowly, such that I thought
    I was in fact shearing the head off. But no, I checked the
    other end, and the bolt was moving. I tapped on both ends as
    best I could, often, too, to help free it. After one turn or
    so, I put a 14-mm combination wrench (closed end) on the
    bolt, doubled it up with my 15 mm combination wrench to get
    more lever arm, and unscrewed the bolt until its end was
    flush with the fixed nut. It was very difficult the whole
    time; pretty hard on the arms, even using pipe etc.
    extensions. I sprayed more PB Blaster into the now exposed
    threads of the nut. Pushed some anti-seize in, and
    re-tightened it. I didn't want to take the bolt out all the
    way, because I thought it possible a part of the car would
    collapse.

    The driver's side bolt had the disadvantage of having the
    oil pan in the way, so I couldn't use the 18-inch breaker
    bar. Eventually I just used the roughly six-inch long 14-mm
    combination wrench (closed end) and a scissors jack (resting
    on some plywood) on its end, tapping on the combination
    wrench throughout to ensure it stayed in place 'round the
    bolt. I shot some spray paint at the bolt end this time to
    make it easier to see the bolt moving. It too came free very
    slowly, but surely. The scissors jack wasn't resisting being
    raised all that much, so I didn't feel it was unsafe, though
    of course I took precautions (safety glasses; thick leather
    gloves at one point; a board between me and the setup for
    awhile). After getting a revolution out of the bolt, I did
    the rest by hand, hanging onto a sturdy part of the exhaust
    pipe at times for leverage.

    Didn't even bother torque-wrenching everything afterwards.
    From experience I feel pretty confident I applied over 43
    ft-lbs (the spec for these bolts).

    Tomorrow I hope to narrow down my ball joint lifter tool
    choices (based on counsel here) and possibly order one.
     
    Elle, May 3, 2006
    #7
  8. Take a relaxation break tonight - you've earned it! Tooth and nail
    mechanics, ya gotta hate it.

    Mike
     
    Michael Pardee, May 3, 2006
    #8
  9. Take a relaxation break tonight - you've earned it! Tooth and nail
    mechanics, ya gotta hate it.

    Mike
     
    Michael Pardee, May 3, 2006
    #9
  10. Elle

    David Guest

    I hate to tell you this, but you probably don't have the bolts loose. I
    just went through the same process on my '91 CRX SI. The problem is the
    bolts fit through a steel sleeve in the middle of the rubber bushing at
    the end of the control arm. The sleeve/bolt interface is supposed to be
    greased "for life" but it isn't so they rust together after many years.
    When you put enough torque on the bolt, you shear the sleeve away from
    the rubber. You can push the sleeve out of the bushing as long as the
    threads on the bolt push against the threads on the nut then you're
    stuck. There are three options. 1) Pay money to a shop to do the job
    for you. 2) drag out the torch and cut the bolts off at both ends, drop
    out the control arm and take it to a shop to have the bushings replaced;
    they are press fit into the control arms and take A LOT of pressure to
    put in. or 3) burn off the nuts, cut off the bolts buy new ones, replace
    the bushings however you decide and reinstall the parts with new nuts
    not welded to the frame.

    BTW You don't have to worry about anything going flying or falling out
    when you do this job. With the car on jack stands, there's no stress on
    the lower control arms and they're pretty tightly wedged into the
    mounts. You will have to pry them out once the bolts are removed and
    they will hang off the spindle end of the suspension.

    If you got lucky and your bolts really did release from the bushings,
    just pull them out, grease the heck out of them with GOOD grease before
    reassembling with the new bushings. If you don't have a hydraulic
    press, you will need to get the old bushings pressed out and the new
    bushings pressed in at a shop so equipped.

    David
     
    David, May 3, 2006
    #10
  11. Elle

    Elle Guest

    Hm, there was something odd going on mid-body of the
    bolt/bushing regions along the lines of what you suggest. I
    gather you tried putting a steel rod against the bolt's free
    end and banging, to push it through, without success.

    On the rear control arms, I am well-acquainted with the
    bushing etc. material seizing on the outboard bolts. The
    rear inboards OTOH were fine and came apart easily enough.

    snip but comments noted
    I am en route purchasing a good ball joint separator tool
    and then seeing if I can get the front control arms
    completely off. Except for the ball joints and the inboard
    bolts, I have had just about everything else attaching to
    the lower control arm dis-assembled.

    I have been contemplating purchase of an A-frame 12-ton
    hydraulic press from Harbor Freight to press out the
    bushings. It's on sale through May for $80. The price is low
    enough to I think justify the purchase.

    Currently studying Mugen bushings (kingmotorsports.com) as
    the replacements. Although a site Tegger mentioned a few
    years ago indicates there's a TSB out on the older bushings,
    and the newer ones Honda sells are better.

    I appreciate your sharing your experience. This is a
    multi-month project, for my education as well as to maintain
    well my 40 mpg 1991 Civic.
     
    Elle, May 3, 2006
    #11
  12. Elle

    Elle Guest

    David is correct. My 91 Civic (176k miles) had the classic
    frozen bolt-to-bushing-sleeve problem. After further
    research on the net, I found this is endemic to several
    other makes of automobiles.

    Fortunately, one thing was something in common to all the
    success stories: Use of an air die grinder or an air angle
    grinder.

    PB Blaster is not enough. Nor is heat, by all reports. A few
    years ago, I tried a cheap-o electric drill with a grinding
    stone ( = low RPM, low power) with my rear suspension, and
    it was hell.

    So get the air die grinder or air angle grinder. The steps I
    took below did not take more than a few hours. I went very
    slowly, since it's been many years since I had any type of
    air grinder in my hand. Also, the space is tight. I tried to
    use the grinder as little as possible, to minimize risk to
    life, limb, and property.

    Steps for removing a front inbd lower arm suspension bolt
    frozen to its bushing sleeve:

    -- Spray with PB Blaster all exposed threads (nut and bolt).
    Dunno if this really helps, but it couldn't hurt.

    -- With a 1/4-inch shank arbor designed for wheels, affix a
    1/16-inch thick, 3-inch diameter "cutoff blade" (= cutoff
    wheel) to an air die grinder. I bought the cutoff wheel and
    arbor as a set from Lowe's for $6. Also pick up for $2 some
    air tool oil. I bought the air die grinder for $13 at
    Checker Auto Parts. In other words, it is about as cheap as
    they make. Make sure the air die grinder RPM rating is lower
    than the wheel rating. Grinding wheels, for one, are known
    to explode if rotated higher than their rating. (Thanks to
    rec.autos.tech for many of these warnings.)

    -- Have safety glasses, face covering, and leather gloves
    handy. If in an enclosed space, wear a dust mask. Don these
    when
    using the air die grinder.

    -- Drive the front of the car onto rhino ramps to give you
    enough space to work.

    -- Do not work beneath a hot engine. For one thing, sparks
    will fly while cutting. A risk of fire exists.

    -- Because the bolt typically seizes to the inner sleeve of
    the bushing, one can unscrew the bolt only until its threads
    no longer engage with the (fixed) nut. Then the bushing
    inner sleeve becomes exposed. Unscrew the bolt until about
    1/2 inch of bushing is exposed. If years have passed since
    the bolts were removed, this will take some effort. I did
    this a few days in advance, just to break the bolt free of
    any seizing in the nut.

    -- With the cutoff wheel, leather gloves, and serious face
    protection (face mask), grind in maybe three steps until the
    sleeve is penetrated and the bolt is exposed.The sleeve is
    1/8-inch thick, so it's not that much grinding. I think this
    took only about two minutes of altogether. Sparks fly, of
    course. I protected the front wheel with blocks of wood. A
    piece of cutoff wheel flying off and penetrating the tire
    would be curtains for you.

    -- Arguably at this point you might want to drive the car
    down the ramps and put the front side on a jackstand. The
    ramps seem more secure to me for heavy torquing.

    -- Continue grinding until you're one-third to a half way
    through the bolt. Stop grinding now and then and tap the
    exposed bolt hard via the groove you've cut in the sleeve.
    Tap on both ends. Apply a wrench and advance (tighten) the
    bolt back into the nut a couple of times. Eventually by
    looking into the new groove in the sleeve, I could see the
    bolt was moving relative to the sleeve. At some point I
    could hear little popping noises, too, indicating the bolt
    was breaking free of the bushing sleeve.

    -- Within a half hour or so, the bolt was free of the
    bushing.

    -- To remove the bolt fully, support the inbd end of the
    control arm with a jack. I managed to strip the threads of
    the bolt while removing it, because I didn't line things up
    carefully. I also knew I had a spare bolt and spare sleeve.

    -- Reinserting a new bolt should be done with the front side
    on a jackstand. This allows adjustment of the wheel
    position, which in turn allows easier adjustment of the
    control arm position. Use a crowbar on top of the control
    arm. Insert a screwdriver into the bolt hole and bushing to
    help things along as needed. One can pull down on the
    control bar and pry with the crowbar and screwdriver until
    the bolt can be inserted into the bushing again. It's a
    little tricky but not aggravatingly so, if one has done it a
    few times.

    I chose not to cut all the way through the sleeve and bolt,
    because I felt overall removal would be easier with an
    intact bolt. The bolt head in particular permits one to
    maneuver the other end of the bolt, but of course only as
    long as they're still attached.
     
    Elle, May 14, 2006
    #12
  13. Elle

    Elle Guest

    David is correct. My 91 Civic (176k miles) had the classic
    frozen bolt-to-bushing-sleeve problem. After further
    research on the net, I found this is endemic to several
    other makes of automobiles.

    Fortunately, one thing was something in common to all the
    success stories: Use of an air die grinder or an air angle
    grinder.

    PB Blaster is not enough. Nor is heat, by all reports. A few
    years ago, I tried a cheap-o electric drill with a grinding
    stone ( = low RPM, low power) with my rear suspension, and
    it was hell.

    So get the air die grinder or air angle grinder. The steps I
    took below did not take more than a few hours. I went very
    slowly, since it's been many years since I had any type of
    air grinder in my hand. Also, the space is tight. I tried to
    use the grinder as little as possible, to minimize risk to
    life, limb, and property.

    Steps for removing a front inbd lower arm suspension bolt
    frozen to its bushing sleeve:

    -- Spray with PB Blaster all exposed threads (nut and bolt).
    Dunno if this really helps, but it couldn't hurt.

    -- With a 1/4-inch shank arbor designed for wheels, affix a
    1/16-inch thick, 3-inch diameter "cutoff blade" (= cutoff
    wheel) to an air die grinder. I bought the cutoff wheel and
    arbor as a set from Lowe's for $6. Also pick up for $2 some
    air tool oil. I bought the air die grinder for $13 at
    Checker Auto Parts. In other words, it is about as cheap as
    they make. Make sure the air die grinder RPM rating is lower
    than the wheel rating. Grinding wheels, for one, are known
    to explode if rotated higher than their rating. (Thanks to
    rec.autos.tech for many of these warnings.)

    -- Have safety glasses, face covering, and leather gloves
    handy. If in an enclosed space, wear a dust mask. Don these
    when
    using the air die grinder.

    -- Drive the front of the car onto rhino ramps to give you
    enough space to work.

    -- Do not work beneath a hot engine. For one thing, sparks
    will fly while cutting. A risk of fire exists.

    -- Because the bolt typically seizes to the inner sleeve of
    the bushing, one can unscrew the bolt only until its threads
    no longer engage with the (fixed) nut. Then the bushing
    inner sleeve becomes exposed. Unscrew the bolt until about
    1/2 inch of bushing is exposed. If years have passed since
    the bolts were removed, this will take some effort. I did
    this a few days in advance, just to break the bolt free of
    any seizing in the nut.

    -- With the cutoff wheel, leather gloves, and serious face
    protection (face mask), grind in maybe three steps until the
    sleeve is penetrated and the bolt is exposed.The sleeve is
    1/8-inch thick, so it's not that much grinding. I think this
    took only about two minutes of altogether. Sparks fly, of
    course. I protected the front wheel with blocks of wood. A
    piece of cutoff wheel flying off and penetrating the tire
    would be curtains for you.

    -- Arguably at this point you might want to drive the car
    down the ramps and put the front side on a jackstand. The
    ramps seem more secure to me for heavy torquing.

    -- Continue grinding until you're one-third to a half way
    through the bolt. Stop grinding now and then and tap the
    exposed bolt hard via the groove you've cut in the sleeve.
    Tap on both ends. Apply a wrench and advance (tighten) the
    bolt back into the nut a couple of times. Eventually by
    looking into the new groove in the sleeve, I could see the
    bolt was moving relative to the sleeve. At some point I
    could hear little popping noises, too, indicating the bolt
    was breaking free of the bushing sleeve.

    -- Within a half hour or so, the bolt was free of the
    bushing.

    -- To remove the bolt fully, support the inbd end of the
    control arm with a jack. I managed to strip the threads of
    the bolt while removing it, because I didn't line things up
    carefully. I also knew I had a spare bolt and spare sleeve.

    -- Reinserting a new bolt should be done with the front side
    on a jackstand. This allows adjustment of the wheel
    position, which in turn allows easier adjustment of the
    control arm position. Use a crowbar on top of the control
    arm. Insert a screwdriver into the bolt hole and bushing to
    help things along as needed. One can pull down on the
    control bar and pry with the crowbar and screwdriver until
    the bolt can be inserted into the bushing again. It's a
    little tricky but not aggravatingly so, if one has done it a
    few times.

    I chose not to cut all the way through the sleeve and bolt,
    because I felt overall removal would be easier with an
    intact bolt. The bolt head in particular permits one to
    maneuver the other end of the bolt, but of course only as
    long as they're still attached.
     
    Elle, May 14, 2006
    #13
  14. Elle

    Elle Guest

    I spoke too soon. While the pass. side bolt came free pretty
    easily, the driver's side today was hell. After hours of
    failure, I ended up purchasing a super-skinny 1/32-inch
    cutoff wheel (rated 18,000 RPM, so I took a risk :-( ) ,
    cut off the bolt head and took another full cut at the bolt
    end side, so the control arm inbd end would swing relatively
    free. I extracted the inner sleeve, with bolt still
    attached, with a C-clamp.

    Subsequently I tried to pound the bolt out of the sleeve at
    my workbench. That sucker isn't moving no way no how...

    I threw a spare bolt and sleeve into the control arm and
    called it a day.

    The bracket that supports the bolt is all banged up but in
    my estimation still quite functional.

    New bushings are supposed to arrive in the mail tomorrow
    from Kingmotorspors.

    I'll say this: Those 1/32-inch cutoff wheels do nearly cut
    high strength steel like butter.
     
    Elle, May 17, 2006
    #14
  15. Elle

    Elle Guest

    I spoke too soon. While the pass. side bolt came free pretty
    easily, the driver's side today was hell. After hours of
    failure, I ended up purchasing a super-skinny 1/32-inch
    cutoff wheel (rated 18,000 RPM, so I took a risk :-( ) ,
    cut off the bolt head and took another full cut at the bolt
    end side, so the control arm inbd end would swing relatively
    free. I extracted the inner sleeve, with bolt still
    attached, with a C-clamp.

    Subsequently I tried to pound the bolt out of the sleeve at
    my workbench. That sucker isn't moving no way no how...

    I threw a spare bolt and sleeve into the control arm and
    called it a day.

    The bracket that supports the bolt is all banged up but in
    my estimation still quite functional.

    New bushings are supposed to arrive in the mail tomorrow
    from Kingmotorspors.

    I'll say this: Those 1/32-inch cutoff wheels do nearly cut
    high strength steel like butter.
     
    Elle, May 17, 2006
    #15
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